@nkresho; that's what I expected to see happen with mine, and I was going to make the assumption that, if that was a common thing, the only reason the new kombi valve fixed the issue, is because in reality, the wires were the issue. Glad you were able to sort it out, and hope whatever you're moving onto treats you well.
@Diggs24; did you have the code masked/whatever so you're not seeing a CEL? If mine comes back, I may go that route.
I'm loathe to suggest that I believe my kombi valve actually failed, because I never saw the pressure sensor show above 14.4# when the system wasn't active and the car was running. I would expect a different code, maybe, for an overpressure issue if that were the case. The fact that the tests check out fine, both on the old valve and new valve, don't really make sense to me.
Like I said, I'll monitor and report back. The only other thing I have going on is the need to do a carbon cleaning soon, but I'm not confident that could cause this issue, surely?